Precision Airgun owner, Chuck Trepes, asked me to modify some new style Benjamin/Sheridan valve stems to work with vintage Benjamin pump guns. Seems the new Sheridans and Benjamins use a fairly normal coil spring inside the check valve, while the older Benjamins used a conical shaped volute spring. The new stems have a post that the spring fits over, but it's too large in diameter for the old conical spring.
What is the #99-079 number on the envelope? I'm going to guess that these are actually Crosman part #397-038. The one on the left has the smaller diameter post that Chuck needs.
As long as I roughly match the diameter, the spring will stay in location.
Really a perfect job for a small lathe like this. The model Chuck provided didn't have any semblance of a truly round post. It varied by several hundredths in diameter. I settled on turning these down to the average diameter.
As long as the volute spring fits over the end, it's a go. This was such a non-precision job, I just used a comparison caliper rather than measure each piece. I was still within about two or three thousandths of an inch over the batch.
I can't find my notes as I write this. Believe I took the diameter to 0.248". I'll find it and edit if necessary. The important part is the spring fit, not the actual number.
In about 20 minutes, I had six done.
Friday, May 7, 2010
Monday, May 3, 2010
Gecado Diana Model 5 Pistol, Fixing The Piston Head
Now to deal with that messed up piston head.
I chucked it in the 3 jaw. You can see the folded over burrs that are keeping the loose head in.
I turned away a couple of thou' at a time. I wanted to remove the minimum.
Then when I had a nice clean ring on the face I started working on the inside rim.
At this point I was able to pop the head out. Those burrs were thick.
The head...
The back side. As you can see it's a rivet of some sort that retained the original seal.
Dialing in the piston in the 4 jaw chuck.
Boring the recess true and clean.
Ready for a head.
The insert roughed out.
Using a form cutter to make the dovetail button. Notice the chatter marks.
Final cutting, chatter removed at very low speed.
You can see the tool I ground. The Diana pistons seem to have a 70 degree dovetail as best I can measure.
Cutting the insert off.
The insert.
Fits!
I soldered it in with soft solder. The new acetylene tank did not catch on fire like the old one did last time. A nice even ring of solder holding the insert in. I cleaned the face up with a very fine pass across the face.
You can see the solder flowed inside.
Using my extremely handy Diana seal tool.
Popping the seal on. Notice I cleaned up the OD near the head as it was a bit scored.
The seal in place. Looks good.
Another shot. I bought the seal from Air Rifle Headquarters. He gets a lot of my money these days.
Now to derust, deburr, clean, reblue the pistol, make breech seal (o-ring) shims, lube and reassemble...then test. Then if it works... fix the cap that screws on the end...all the ones I have are beat up and I should make a threaded arbor so I can reknurl/cut new knurls after truing. fix the stock... fix the windage screw... I'll never run out of projects.
I chucked it in the 3 jaw. You can see the folded over burrs that are keeping the loose head in.
I turned away a couple of thou' at a time. I wanted to remove the minimum.
Then when I had a nice clean ring on the face I started working on the inside rim.
At this point I was able to pop the head out. Those burrs were thick.
The head...
The back side. As you can see it's a rivet of some sort that retained the original seal.
Dialing in the piston in the 4 jaw chuck.
Boring the recess true and clean.
Ready for a head.
The insert roughed out.
Using a form cutter to make the dovetail button. Notice the chatter marks.
Final cutting, chatter removed at very low speed.
You can see the tool I ground. The Diana pistons seem to have a 70 degree dovetail as best I can measure.
Cutting the insert off.
The insert.
Fits!
I soldered it in with soft solder. The new acetylene tank did not catch on fire like the old one did last time. A nice even ring of solder holding the insert in. I cleaned the face up with a very fine pass across the face.
You can see the solder flowed inside.
Using my extremely handy Diana seal tool.
Popping the seal on. Notice I cleaned up the OD near the head as it was a bit scored.
The seal in place. Looks good.
Another shot. I bought the seal from Air Rifle Headquarters. He gets a lot of my money these days.
Now to derust, deburr, clean, reblue the pistol, make breech seal (o-ring) shims, lube and reassemble...then test. Then if it works... fix the cap that screws on the end...all the ones I have are beat up and I should make a threaded arbor so I can reknurl/cut new knurls after truing. fix the stock... fix the windage screw... I'll never run out of projects.
Subscribe to:
Posts (Atom)